I think that I am in the clear.
Here is what happened.
I first called Adavanced auto parts and they said that the hose was a dealer part and I'd need to call the dealership.
I called the dealership and they said they had to order the hose (which was actually fine) but had the connector. I was able to pick them up Friday.
I asked some friends at work and another suggestion was to try to get a diamond punch to bite on the inside lip of the threads and get er spinning out that way. I thought this sounded like a good idea to try before using the hacksaw blade.
I called all around trying to find a diamond punch bit nobody in town had one. I called back over to Advanced Auto Parts and got someone on the line who new 2 whits about my problem. He said he had a prick punch which I might be a ble to use. Also suggested a liquid teflon thread sealer to seal the fitting. He also had for me a solid steel fitting that was much beter than the aluminum piece of crap the dealership sold me. Almost 10$ less expensive too!
I tried the punch but it was hopeless. I had a cheapo chisel that i bought 2 for 1$ at the dollar store for just some purpose as to mangle on a project like this. It seemed to wedge perfevtly down inside the opening. I managed to get the tang loose from the handle and proceeded to chuck the tang of the chisel into my brace and bit.
I torqued down that brace real good onto the chisel. It was set firm up inside the broken off stump off the old fitting. I huffed and i puffed but i could not get that sucker to budge. I sprayed in some more solvent and walked away. Let it soak real good. Went to pick the wife up from work (since i had her car all day) came home and drank a beer. Anyway i got back too it and the chisel broke free.
I took to the hack saw. I cut through in 2 spots. Pried out the first piece , then cut the 3rd slot and removed the last two pieces of threading. I wedged the shop vac hose over the area where i worked to make sure no debris fell in the manifold. Sombody warned that a chunk of that threading could cause a blockage, so i took care to see that all sections of the threading were removed by hand.
I coated the bottom 1/4 inch of the fitting with the thread sealer. It was a bear to get threaded. All i have to use is a cresent wrench. I am gonn see if a friend has a socket big enough to fit over it to get it threaded further (if he feels it needs to be).
I have driven the truck and the temp seems fine and the fitting seems to be holding as well as the seal. Can anyone think of anything else i need to check? I'll try to folow up with a pic of the new fitting in place.
thanks again for the help Dan,
now I can get back to my woodworking. If you have any carpentry questions i am there for ya'
cheers